Thoughts on Races 4&5 (6/25) 06/26/2009
Well, what an eventful day it was. It began ok when we were ready a half hour early, because it's nice to not have to rush around before we go. On the way out, I'm following my brother's trailer, and I figure out that I have no trailer brakes. After a slow ride to the gas station and the smell of hot rotors coming from my truck, I search the entire wiring system to see why I don't have brakes. I worked on that truck and trailer for 30 minutes, and couldn't figure out what the problem was. Frustrated and late, I got back in the truck and headed out. Wouldn't you know, the damn brakes work again. So, I have no idea what I did, but I did something. Add Comment Thoughts on Race 3 (6/4) 06/05/2009
What a mess this race was. We didn't even make it past turn 1 before cars were wrecked. We did so well the last race! I didn't have a good feeling about this race heading into it. I just was not into racing for some reason. I was just shifting into 3rd gear when the #68 was turned around right in front of me. I had someone on the high side really crowding me, I thought I was going to hit him, but instead I got hit on the left by the #04. That was the first time while racing at Thompson that I thought, "It's over, I'm toast". You know what, there's not really a lot of damage to my car, but he got me pretty solid. I whacked my head off my left headrest pretty good, and my foot slipped over to my clutch pedal so when I went to hit the brakes again, I pushed the clutch in. Awkward. Needless to say, I wasn't sure if the car was damaged bad or not because it was a pretty solid hit. I brought it down the pit road to the photographers and firemen, and I asked them how bad it was. They looked it over and said it was ok, so I went back out. I knew there was something wrong with the front end, but I decided to tough it out. The first corner under speed was kind of sketchy, but after a while, I started to figure it out. It was really boring sitting back in the pack because the car wouldn't handle. I measured the toe this afternoon, and I found out that it got knocked in 1/8". That would explain why it developed a loose condition. | AuthorBrent Gleason, Driver of Thompson Mini Stock #4, keeps a log of his career ArchivesOctober 2011 Categories |
RSS Feed